全球航空器事故数据

时间区间

1902-2024


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全球航空器事故数据-英文字段全球航空器事故数据-中文字段
Year年份
Date日期
Time时间
Type机型
Owner/operator所有者/经营者
Registration飞机号
MSNMSN
Year of manufacture制造年份
Engine model发动机型号
Fatalities死亡人数
Other fatalities其他死亡人数
Aircraft damage飞机损坏情况
Category事件类型
Location地理位置
Phase出事阶段
Nature飞机用途
Departure airport始发机场
Destination airport到达机场
Confidence Rating信用评级
narrative事件说明
notes备注
Cycles飞行次数
Total airframe hrs总飞行时长
Report number报告编号
Investigating agency调查机构
Download report下载报告
Accident investigation PDF调查报告
Status调查进度
Duration调查时长

样本数据

YearDateTimeTypeOwner/operatorRegistrationMSNYear of manufactureEngine modelFatalitiesOther fatalitiesAircraft damageCategoryLocationPhaseNatureDeparture airportDestination airportConfidence RatingnarrativenotesCyclesTotal airframe hrsReport numberInvestigating agencyDownload reportAccident investigation PDFStatusDuration
年份日期时间机型所有者/经营者飞机号MSN制造年份发动机型号死亡人数其他死亡人数飞机损坏情况事件类型地理位置出事阶段飞机用途始发机场到达机场信用评级事件说明备注飞行次数总飞行时长报告编号调查机构下载报告调查报告调查进度调查时长
2020Saturday 25 April 202012:15Aeronca 7AC ChampionPrivateN832167AC-18771946Continental A65-8FFatalities: 0 / Occupants: 10SubstantialAccidentEnosburg, VT - United States of AmericaLandingPrivateSouth Hero, VT (VT26)Enosburg, VTAccident investigation report completed and information capturedThe pilot reported that, during the landing roll on a private grass airfield, the main landing gear dug into soft grass, and the airplane nosed over. The airplane sustained substantial damage to the right-wing lift strut. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. Probable Cause: The pilot's improper decision to land on unsuitable terrain, which resulted in a nose-over.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description4573 hoursERA20CA159NTSBFinal reportdba924a4b33c6d6359c9baa63c062249Investigation completed3 months
2020Wednesday 5 August 2020Javelin WichawkFatalities: 0 / Occupants: 10SubstantialAccidentLismore Airport, NSW (YLIS) - AustraliaUnknownPrivateLismore Airport, NSW (YLIS)Information verified through data from accident investigation authoritiesDuring landing in wet grass parallel to the runway, the wheels dug into soft ground and the aircraft pitched over coming to rest inverted. The aircraft was substantially damaged and the pilot sustained minor injuries.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionATSB
2020Sunday 16 August 202014:54 UTCAerotechnik L-13SEH VivatPrivateN334BA9405171994Fatalities: 0 / Occupants: 20SubstantialAccidentWilliam 'Tiny' Zehnder Field Airport (66G), Saginaw County, MI - United States of AmericaTake offPrivateFrankenmuth, MI (66G)Frankenmuth, MI (66G)Accident investigation report completed and information capturedThe pilot reported that following a landing and back-taxi in a motor glider, he failed to stow the speed brake prior to attempting a subsequent takeoff. During the takeoff attempt, the glider would not climb out of ground effect. The motor glider departed the end of the runway and impacted terrain which resulted in substantial damage to the fuselage. Probable Cause: The pilot's failure to stow the speed brake prior to attempting takeoff.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionCEN20CA337NTSBFinal report333be449d713f47f063f5d8eb3392e47Investigation completed
2020Tuesday 27 October 202010:33 LTHughes 369DWindward Aviation IncN58251880317D1978Rolls Royce 250-C20BFatalities: 0 / Occupants: 10SubstantialAccidentnear Nuuanu Reservoir, Honolulu, Oahu, HI - United States of AmericaEn routeCargoOahu-Dillingham Airfield, HI (HDH/PHDH)Kahului Airport, HI (OGG/PHOG)Accident investigation report completed and information capturedDuring longline operations, the helicopter lost partial power and the main rotor rpm decreased. The pilot jettisoned the external load and the helicopter impacted trees, resulting in substantial damage. The engine continued to run after impact, and the pilot performed an emergency engine shutdown. Examination revealed that the start fuel pump was damaged. The circlip and pin that held the flapper valve in place in the bypass inlet were missing, and the flapper valve was wedged against the sidewall of the bypass inlet, obstructing about 50% of the discharge port. The pin was located in the fuel line between the start fuel pump and the engine-driven fuel pump; the circlip was not found. No other mechanical malfunctions were found that would have precluded normal operation. The pin found in the fuel line and obstruction from the flapper valve located in the start fuel pump likely induced restricted fuel flow from the engine-driven fuel pump to the engine, which resulted in a partial loss of engine power. Based on the available evidence, the reason for the separation of the circlip from the pin could not be determined. Probable Cause: A partial loss of engine power due to an obstructed fuel line as a result of the separation of the circlip from the pin used on the fuel start pump. The reason for the circlip separation could not be determined based on the available evidence.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description20345 hoursANC21LA003NTSBFinal report21e3d60d08948f010ee098e5ac7f175fInvestigation completed1 year and 8 months
2020Friday 21 August 2020Pilatus PC-12/45Fat City Air Service LLCN8YU4132001P&W Canada PT6A-67Fatalities: 0 / Occupants:0UnknownAspen Pitkin County Airport (ASE/KASE), CO - United States of AmericaTaxiUnknownInformation is only available from news, social media or unofficial sourcesAircraft struck Raytheon Hawker 800, N489BM, while taxiing.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2020Thursday 2 January 202010:25Cirrus SR22 GTSCornerstone Aviation LLCN323SR22712006Continental IO-550-NFatalities: 0 / Occupants: 20SubstantialAccidentKenansville, NC - United States of AmericaEn routePrivateWorcester Airport, MA (ORH/KORH)Elizabethtown-Curtis L Brown Jr Field, NC (KEYF)Accident investigation report completed and information capturedThe pilot reported that, during a cross-country flight, he heard a pop from the engine, and it subsequently stopped producing power; however, the engine continued to run, and the propeller continued to rotate. The pilot attempted to troubleshoot the loss of power; however, power was not restored. Subsequently, the pilot activated the airplane’s parachute system and the airplane impacted trees and terrain, resulting in substantial damage to the airframe. Postacccident examination of the engine revealed that the camshaft fractured at one of its four oil transfer holes. As a result, camshaft continuity was lost, and the engine was partially unable to produce power. Forensic examination of the fracture surface revealed that the fracture occurred due to fatigue that initiated from a burr at the corner of an oil transfer hole. The extent of fatigue crack growth through the cross-section suggested the overall torsion load on the camshaft was relatively low as the crack grew. However, a burr at the edge of a hole is a feature that is known to reduce component fatigue life. The burr was deformed and coated, consistent with forming during a peening operation and before the manganese phosphate coating had been applied. A similar burr was also observed on the adjacent oil transfer hole in the camshaft. The presence of a burr suggests the corner of the hole was not properly broken before the part was peened during manufacturing, leading to deformation of a sharp corner during the peening operation. Probable Cause: A fatigue failure of the camshaft due to a manufacturing defect, which resulted in a partial loss of engine power.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information. Corrections or additions? ... Edit this accident description3774 hoursERA20LA064NTSBFinal report9bb962bf5514931a56ca757cc4cd45caInvestigation completed2 years and 3 months
2020Saturday 9 May 202011:10 LTAyres S-2R-G1 Turbo ThrushFarmers ServicesN2245SG1-106Airesearch TPE331Fatalities: 0 / Occupants: 10SubstantialAccidentImperial County Airport (KIPL/IPL), CA - United States of AmericaLandingAgriculturalImperial County Airport, CA (IPL/KIPL)Imperial County Airport, CA (IPL/KIPL)Accident investigation report completed and information capturedShortly after landing, the airplane veered left. The pilot used right rudder and applied right brake to counteract the turn, and the airplane began to straighten out. Immediately after, he felt that the right brake was not working, and the airplane again made an immediate turn to the left. The airplane exited the left side of the runway, the left-wing tip impacted the ground, and the airplane spun to the left, which resulted in a collapse of the left main landing gear and substantial damage to the left wing. An examination of the right brake assembly revealed that the center piston O-ring was damaged, and the right brake hydraulic fluid reservoir was empty. These discrepancies resulted in the loss of brake pressure and subsequent failure of the right brake. Probable Cause: The pilot's loss of control during a landing roll due to a failure of the main O-ring in the right brake assembly, which resulted in a loss of brake pressure and subsequent brake failure.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionWPR20LA172NTSBFinal reportb5c6b969882f429aca48aedaaf224c9aInvestigation completed2 years 1 month
2020Thursday 17 September 2020c. 10:21Cessna 152 IILahore Flying Club (LFC)AP-BEO15285762Fatalities: 0 / Occupants: 10MinorAccidentLahore/Walton Airport (OPLH) - PakistanLandingTrainingAllama Iqbal International Airport LahoreLahore/Walton (OPLH)Information is only available from news, social media or unofficial sourcesThe nose landing gear collapsed on touchdown. The first solo student pilot was not injured. Preliminary information suggests the pilot was making video/taking photos of the flight including landing.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2020Monday 8 June 2020Airbus A350-941LATAM BrasilPR-XTI2502018Rolls-Royce Trent XWB-84Fatalities: 0 / Occupants:0MinorSão Paulo-Guarulhos International Airport, SP (GRU/SBGR) - BrazilStandingPassengerInformation is only available from news, social media or unofficial sourcesA LATAM Airlines Brasil Airbus A350-900 suffered minor damage to the no.2 engine fan cowl when a vehicle impacted the nacelle during ground operations.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2020Friday 10 January 202012:40 LTMil Mi-8TKrasAviaRA-22901984200921984Fatalities: 0 / Occupants: 170IncidentKrasnoyarsk Krai, Siberia - RussiaEn routePassengerSyndasskoKhatangaInformation verified through data from accident investigation authoritiesThe helicopter made an emergency landing after engine failure. There are said to be no fatalities.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information. Corrections or additions? ... Edit this accident description
2020Monday 5 October 202011:15Cessna 180 SkywagonFatalities: 0 / Occupants:0SubstantialAccidentSaarmund Airport (EDCS) - GermanyTake offUnknownSaarmundInformation verified through data from accident investigation authoritiesDuring takeoff roll, the aircraft collided with a deer running across the runway.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionBFU
2020Sunday 29 March 2020Luscombe 8APrivateN718993326Fatalities: 0 / Occupants: 10Unknown24330 Snake River Rd, Asotin, WA - United States of AmericaLandingUnknownInformation is only available from news, social media or unofficial sourcesThe aircraft experienced a loss of directional control and subsequent runway excursion upon landing at Snake River Rd, Asotin, Washington. The airplane came to rest inverted, sustaining unspecified damage, and the sole pilot onboard was not injured.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2020Tuesday 4 August 2020Harbin Y-12-IIKenya Air Force - KAFKAF12800971997Fatalities: 0 / Occupants: 100SubstantialAccidentDhobley Airstrip - SomaliaTake offMilitaryDhobley AirstripNairobi-Moi Air Base (HKRE)A Kenya Air Force Harbin Y-12-II suffered an accident at Dhobley Airstrip in Somalia. There were no serious injuries to the 10 people on board but the aircraft was seriously damaged. The landing gear as well as the left-hand wing have collapsed. The accident happened after the aircraft had taken off from Dhobley Airstrip after delivering supplies to U.N. Amisom forces.
2020Monday 20 January 202012:20Cessna 150GPrivateN4763X150648131966Continental O-200 SERIESFatalities: 1 / Occupants: 10DestroyedAccidentnear Cherokee County Airport (JKV/KJSO), Jacksonville, TX - United States of AmericaEn routePrivateJacksonville-Cherokee County Airport, TX (JKV/KJSO)Accident investigation report completed and information capturedOn January 20, 2020, about 1220 central standard time, a Cessna 150G airplane, N4763X, was substantially damaged when it was involved in an accident near Jacksonville, Texas. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. Radar information showed that, after departing in day visual meteorological conditions, the pilot climbed the airplane to a maximum altitude of about 1,600 ft mean sea level (msl) before entering a gradual descent. The last radar return showed the airplane at a speed of 92 knots and altitude about 900 ft msl. The wreckage was found in the vicinity of a 1,586-ft-tall television tower, and its distribution was consistent with the left wing contacting one of the tower’s guy wires, resulting in a separation of the outboard section of the left wing. The airplane subsequently impacted terrain in a nose-down, near vertical attitude and was destroyed by impact. Examination revealed no evidence of mechanical malfunctions or anomalies that would have precluded normal operation of the airplane or engine. The circumstances of the accident are consistent with the pilot’s failure to maintain clearance from tower guy wires while flying at low altitude. Probable Cause: The pilot’s failure to maintain clearance from guy wires associated with a tower while maneuvering at low altitude.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionWPR20FA067NTSBFinal reportb085a33513575b2602831c2fc024b777Investigation completed2 years and 4 months
2020Friday 25 September 202017:30 LTPiper PA-46R-350T MatrixCoadmere IncN920X46922062014Lycoming TIO-540-AE2AFatalities: 0 / Occupants: 20SubstantialAccidentnear Rogers Municipal Airport (ROG/KROG), Benton County, AR - United States of AmericaEn routeTrainingRogers Municipal Airport-Carter Field, AR (ROG/KROG)Rogers, ARAccident investigation report completed and information capturedThe pilot reported that while practicing slow flight and approach-to-stall maneuvers at 5,500 ft msl with the landing gear and flaps fully extended, the stall warning horn sounded, and the airplane began buffeting. The pilot advanced the throttle and lowered the nose of the airplane to recover from the maneuver, when the right wing dropped, the airplane rolled over inverted, and subsequently entered a right spiral dive. The pilot reported that after 5 to 7 turns he regained control of the airplane leveling at 500 to 700 ft agl. The pilot returned to the airport and landed without further incident. Postaccident examination revealed the airplane sustained substantial damage to the fuselage above the left wing's trailing edge, below and forward of the empennage, above the right horizontal stabilizer, and at the tail cone below the right and left horizontal stabilizers. The pilot reported there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. Probable Cause: The pilot's inadvertent loss of aircraft control, resulting in substantial damage to the airframe during the spin recovery.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description815 hoursCEN20LA430NTSBFinal reportb19d985dc8ac7e587ad33e7ec2946c1fInvestigation completed12 months
2020Saturday 25 April 202011:00Fly Synthesis StorchAeroklub “Josip Križaj” AjdovščinaS5-PFAF1BC4940C32KFatalities: 0 / Occupants: 21DestroyedAjdovščina - SloveniaEn routePrivateAjdovšcina Airport (LJAJ)Ajdovšcina Airport (LJAJ)Information is only available from news, social media or unofficial sourcesA paraglider collided with a Fly Synthesis Storch ultralight. Both crashed. The aeroplane pilot pulled the rescue parachute however they were flying to low for the parachute to fully deploy. The two occupants of the ultralight plane suffered heavy casualties but survived the crash. The paraglider died in the crash.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2020Wednesday 2 December 202009:25Boeing 737-529Air DjiboutiEY-56026538/22981992CFMI CFM56-3B1Fatalities: 0 / Occupants: 390Substantial, repairedAccidentGarowe Airport (GGR) - SomaliaLandingPassenger - ScheduledHargeisa Airport (HGA/HCMH)Garowe Airport (GGR/HCMW)Information verified through data from accident investigation authoritiesAn Air Djibouti Boeing 737-529, EY-560, suffered a right-hand main landing gear collapse on landing at Garowe Airport, Puntland, Somalia. The aircraft operated on a flight from Djibouti to Mogadishu, Somalia, with en route stops at Hargeisa and Garowe. The pilot conducted a visual approach and the aircraft was stable. At low altitude the aircraft experienced a windshear and hit the runway hard. The root cause of the accident is loss of control of aircraft. The contributory factor was windshear.42964 hours
2020Tuesday 7 July 202014:35Schleicher ASW-19BOK-798419420Fatalities: 0 / Occupants: 10SubstantialAccidentHodkovice (LKHD) - Czech RepublicLandingPrivateHodkovice nad Mohelkou Airport (LKHD)Hodkovice nad Mohelkou Airport (LKHD)Accident investigation report completed and information capturedOn landing, the aircraft bounced several times and then touched down hard. This caused damage to the nose, the cockpit glazing and the tail. The cause of the accident was most likely the pilot changing the control lever of the aerodynamic brakes and the landing gear lever. As a result, the approach and landing took place at high speeds. The pilot did not successfully solve this situation.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionUZPLNFinal report13201a6d9baf3a4335cefcbd0a8e9e8dInvestigation completed8 months
2020Saturday 30 May 202019:32Cessna 182C SkylaneSkyConceptD-EYST524781959Fatalities: 0 / Occupants: 10DestroyedAccidentLangenhahn, Rhineland-Palatinate - GermanyApproachParachutingAilertchen Airfield (EDGA)Ailertchen Airfield (EDGA)Accident investigation report completed and information capturedAfter dropping four parachutists, the engine failed during descent. Subsequently, the aircraft collided with an overhead power line and crashed into the roof of a residential building. The pilot was injured and the aircraft destroyed. Also the electricity of 50.000 people was cut off. Conclusions: The accident was caused by the pilot experiencing an engine failure due to an interrupted fuel supply, and the aircraft colliding with obstacles during the subsequent emergency landing. The following factors contributed to the accident: - Non-compliance with the manual requirements for the descent procedure with the low fuel quantity present in the wing tanks - Attempts to start the engine without first selecting and approaching an emergency landing area - Too low an altitude at the time of engine failure to safely reach the airport in a glideYou can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionBFUFinal reportbc49249ed207b196706bd1d8da40f09eInvestigation completed3 years and 3 months
2020Sunday 11 October 202014:42Cessna FRA150L AerobatPrivateG-CIIRFRA150001871973Continental O-240-AFatalities: 1 / Occupants: 10DestroyedAccidentNorth of Troutbeck, between Keswick and Penrith, Cumbria - United KingdomTake offPrivateTroutbeck Airfield, Keswick, CumbriaRepton/Gamston Airport (EGNE)Accident investigation report completed and information capturedThe aircraft, a Cessna FRA150L Aerobat (G-CIIR) landed at Troutbeck Airfield with its pilot and a passenger without the required permission. As the conditions on the day meant the aircraft’s takeoff performance from Troutbeck would be marginal, the airfield owner instructed the pilot to depart solo in order to improve the aircraft’s performance by reducing its takeoff weight. On the subsequent takeoff the aircraft was seen to depart controlled flight seconds after getting airborne and strike the ground. The pilot was fatally injured. The investigation identified a number of shortcomings with the preparation for the flight that contributed to the accident. In addition, opportunities were missed to prevent the accident because the pilot did not heed the advice not to operate into grass, performance-limiting airfields, did not obtain PPR and was probably not on the correct radio frequency on arrival. It is likely that the pilot did not fasten his shoulder harness, against the strong advice of his instructor, and this action may have meant the accident became unsurvivable. Flying for any pilot is a continual learning process whether they are newly qualified or very experienced. However, newly qualified pilots should be very careful to make sure they fly within the limits of their experience. This accident highlights the fact that thorough preparation is essential for every flight, and accidents can happen if short cuts are taken or good advice is not heeded. =Damage sustained to airframe= Per the AAIB Report the airframe was "Destroyed". The CAA agreed with this conclusion, as the registration G-CIIR was cancelled, and the airframe de-registered, on 18 May 2021 as "destroyed"You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionAAIB-26991AAIBFinal report117fca6eda4446b661c31e1c7c2016b0Investigation completed1 year 1 month
2020Wednesday 18 March 202013:30Boeing 737-33AAerolínea EstelarYV-642T27267/26001994CFMI CFM56Fatalities: 0 / Occupants: 1180Cacique Aramare Airport (SVPA), Puerto Ayacucho, Amazonas - VenezuelaEn routePassenger - ScheduledBuenos Aires/Ezeiza-Ministro Pistarini Airport, BA (EZE/SAEZ)Caracas-Simón Bolívar International Airport (CCS/SVMI)Information is only available from news, social media or unofficial sourcesEstelar Flight ES-8568 with 118 passengers on board, (crew members not available) was diverted to Puerto Ayacucho’s Cacique Aramare Airport due pressurisation system issues, according to airline statements. Landed safely at 13:30 local time (17:30 Z).This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2020Friday 28 August 2020c. 1045 UTCde Havilland Canada DHC-8-402Q Dash 8SpiceJetVT-SUL4400P&W Canada PW150Fatalities: 0 / Occupants:0Serious incidentCochin International Airport (COK/VOCI) - IndiaApproachPassenger - ScheduledBengaluru (Bangalore) International Airport (BLR/VOBL)Cochin International Airport (COK/VOCI)Information verified through data from accident investigation authoritiesSpiceJet flight SG7077, a DHC-8-402Q (VT-SUL) and Qatar Airways flight QR7477, an Airbus A320-232 (A7-AHA) were involved in a serious airprox incident while on approach to Cochin Airport, India. Minimum separation was reduced to 2 NM horizontally and 500 feet vertically. Probable Cause of the Incident. Non adherence to ATC instructions by the crew of SEJ7077. Contributory factor: During descent to 3000 ft , pilot flying did not engage ‘ALT SEL’ and the same was not monitored by Pilot monitoring also.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionAAIB IndiaFinal reportc59c52e0ef151797c749880cb481ef46Investigation completed6 months
2020Monday 28 December 202020:45 LTBeechcraft B80 Queen Air 8800Bemidji Aviation ServicesN134BALD-2021964Lycoming IGSO-540-B1AFatalities: 0 / Occupants: 10SubstantialAccidentChandler Field Airport, Alexandria, MN - United States of AmericaTake offUnknownChandler Field (AXN/KAXN), Alexandria, MNMinneapolis-St. Paul International Airport, MN (MSP/KMSP)Accident investigation report completed and information capturedThe pilot reported that the takeoff was conducted below the airplane's maximum gross weight. Although his written statement and interviews indicated that there was no frost on the airplane during his preflight examination, the police report of the accident stated that the pilot told the responding officer immediately after the accident that there could have been frost on the wings of the airplane. The airport manager who responded to the accident scene reported that all airplane surfaces were covered with frost when he arrived a short time after the accident. The pilot reported that during the takeoff the rotation speed was between 82 and 85 knots. The pilot's reports of what happened after rotation were consistent, indicating that the airplane began to veer to the right and began shaking. The pilot stated that he did not hear a stall warning and that the airplane did not feel like it was in a stall. While the pilot tried to correct the veering to the right, the airplane pitched down, turned left, and the left wing struck the ground. The airplane then bounced, the right wing struck the ground, and the right main landing gear collapsed. The left wing sustained substantial damage. Airplane performance data indicated that the proper rotation speed for a maximum gross weight takeoff was 96 knots. The power-on stall speed at maximum gross weight for the airplane with landing gear extended and flaps retracted was not specifically listed but would have been between 78 and 91 knots based on available performance data from the airplane owner's manual. In addition, the performance data would have been for an airplane without frost on it; frost would have increased the speed. Based on the available evidence it is likely that the airplane had frost contamination, which the pilot ignored. He then rotated the airplane during the maximum gross-weight takeoff at a speed below the airplane manufacturer's recommended rotation speed. The slower speed in combination with degraded performance due to frost contamination of the airplane's flying surfaces resulted in exceedance of the critical angle of attack, resulting in an aerodynamic stall and subsequent impact with the ground. Probable Cause: The pilot's decision to attempt takeoff with frost covering the airplane and rotating below the published rotation speed, which led to exceedance of the airplane's critical angle of attack and an aerodynamic stall.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description18126 hoursCEN21LA101NTSBFinal report501eed514ef6664c97e0abb0c88f6acfInvestigation completed
2020Saturday 31 October 202014:00Robin DR.400/140BVliegclub Rotterdam (VCR)PH-NSC26112006Fatalities: 0 / Occupants:0MinorAccidentRotterdam/The Hague Airport (RTM/EHRD) - NetherlandsLandingUnknownRotterdam/The Hague Airport (RTM/EHRD)Rotterdam/The Hague Airport (RTM/EHRD)Information verified through data from accident investigation authoritiesDuring landing the pilot lost control of the aeroplane, whereupon it veered off the runway and hit a PAPI light unit with the left wing, before it came to a stop.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionDutch Safety Board
2020Sunday 14 June 2020Schempp-Hirth Ventus 2BOY-HXB72Fatalities: 0 / Occupants: 10SubstantialAccidentHammer (EKHM)r - DenmarkTake offPrivateHammer (EKHM)Hammer (EKHM)Information verified through data from accident investigation authoritiesDuring the winch launch for a thermal flight the glider got a strong crosswind shortly after take off in about 2 meters height. One wing got ground contact and the glider turned and hit the ground hard. The AIBN has identified the following factors that are presumed to have influenced the course of events: - A language barrier, between the winch driver (who was of foreign origin and had limited Danish skills) and the pilot, may have resulted in a misunderstanding about the pilot's intention of a good acceleration at the beginning of the start but a minor move later. - The winch manager's current training condition is estimated during the course of events to have affected the winch operator's operation of the winch. - The glider had a smaller rear rudder effect at low speeds compared to other types of gliders. - Poor acceleration resulted in a long starting run at low speed. The fact that the glider got into the air, at a relatively low speed, may have made it more difficult for the pilot to control the glider. - The glider may have been in lateral imbalance. The center of gravity of the left wing was possibly further located than the center of gravity of the right wing, due to water that had moved outwards in the wing. - A markedly variable headwind component, due to offensive winds from changing directions, probably caused the glider to unexpectedly lose lift. - A subsequent skewed winch move led to loss of control of the glider from low flight altitude. - The pilot did not interrupt the start of the winch launch in time and disconnected from the starting wire.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionHCLJFinal report30d3a195c0d482dc124d0c32666dc73eInvestigation completed8 months
2020Wednesday 30 September 202016:28Robinson R22PrivateFatalities: 0 / Occupants: 10SubstantialAccidentHawkwood, W of Maryborough, QLD - AustraliaEn routeAgriculturalInformation verified through data from accident investigation authoritiesDuring aerial mustering operations, the engine lost power and the helicopter was unable to maintain height. The helicopter made contact with trees and subsequently collided with terrain resulting in substantial damage. The pilot was uninjured.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionATSB
2020Saturday 31 October 2020Cessna TU206C Super SkywagonprivateC-FMQGU20611011968Continental TSIO-520-CFatalities: 0 / Occupants: 10SubstantialAccident28 nm NNW of Bella Coola (CYBD), BC - CanadaEn routePrivateAnahim Lake (CAJ4), BCBella Coola (CYBD), BCInformation verified through data from accident investigation authoritiesA privately operated Cessna 206 aircraft, was conducting a flight from Anahim Lake (CAJ4), BC to Bella Coola (CYBD), BC with a sole pilot on board. While the aircraft was flying at approximately 2000 feet ASL, over the Dean Channel, the engine (Teledyne Continental TSIO-520 -C) experienced a complete power loss. The aircraft was ditched into the channel near the mouth of the Dean River. Upon entry into the water the aircraft began to sink and the pilot quickly exited. The pilot was wearing a manual inflation PFD which he inflated upon exit from the aircraft. The aircraft then sank below the water surface while the pilot, wearing his PFD, swam to the shore line where he was able to summon assistance from a nearby cabin. The pilot sustained minor injuries. An ELT signal was not received.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionTSB
2021Tuesday 24 August 202110:09 LTPilatus PC-21Pilatus FlugzeugwerkeHB-HZD1022005Fatalities: 0 / Occupants: 20Serious incidentEmmen - SwitzerlandUnknownTrainingBuochs Airport (BXO/LSZC)Buochs Airport (BXO/LSZC)Information verified through data from accident investigation authoritiesA Pilatus PC-21 (HB-HZD) and a Cessna 182T (HB-TLM) were involved in a serious airprox incident near Emmen, Switzerland. The two aircraft were at approximately the same altitude with converging flight paths, leading to a dangerous airprox.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionSTSB
2021Thursday 10 June 202119:10Piper PA-32-260 Cherokee SixG&M Aircraft IncN3793W32-7201966Lycoming O-540-E4B5Fatalities: 0 / Occupants: 20SubstantialAccidentnear Lafayette, CO - United States of AmericaEn routeTrainingBroomfield-Rocky Mountain Metropolitan Airport, CO (BJC/KBJC)Lafayette, COAccident investigation report completed and information capturedThe purpose of the instructional flight was for the pilot to receive a checkout in the airplane. Before the flight, the right wing main fuel tank contained 16-18 gallons of fuel, the left wing main fuel tank contained less than 10 gallons of fuel, and both wingtip tanks were completely full (17 gallons each). The pilot and his flight instructor discussed the fuel status before departure and had agreed to operate the engine on the right wing main tank to correct the fuel imbalance between the tanks during the flight. The flight consisted of visual flight rules maneuvers and touch-and-go landings, and about 1.1 hour into the flight the airplane had a loss of engine power about 1,000 ft above the ground while in cruise flight. A forced landing was completed to a nearby field, but shortly after touchdown the airplane collided with a berm that caused the airplane to become airborne again. The nose landing gear collapsed and both wings were substantially damaged when the airplane landed hard the second time. The pilot and his flight instructor both reported that the entire flight had been flown using fuel from the right wing main fuel tank. Neither the pilot nor his flight instructor switched fuel tanks after the loss of engine power because they were focused on the forced landing. The pilot stated that based on the airplane’s performance data, the loss of engine power was likely due to fuel starvation. An onsite examination of the wreckage revealed that the right wing main fuel tank was intact and contained less than ¼ gallon of fuel. According to the airplane’s owner’s handbook, there was about 1 pint of unusable fuel in each of the 4 fuel tanks. The remaining 3 fuel tanks contained usable fuel. Additionally, there were no mechanical malfunctions identified with the airplane’s fuel system or the engine that would have precluded normal operation. Probable Cause: The flight crew’s improper fuel management that resulted in fuel starvation and the loss of engine power.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description3420 hoursCEN21LA261NTSBFinal reportc9c2c7383592781ec2676b5075225098Investigation completed6 months
2021Thursday 30 December 202122:00 UTCATR 72-202 (QC)Calm AirC-FJCQ311P&W Canada PW124BFatalities: 0 / Occupants:0Unknown150 nm WSW of Rankin Inlet (CYRT), NU - CanadaEn routeUnknownGjoa Haven Airport, NU (YHK/CYHK)Thompson Airport, MB (YTH/CYTH)Information verified through data from accident investigation authoritiesAn ATR 72-200 operated by Calm Air, was conducting flight CAV468 from Goa Haven (CYHK), NU to Thompson (CYTH), MB. When the flight was approximately 150 nm west southwest from Rankin Inlet (CYRT), NU, the crew observed an intermittent low oil pressure warning light on the left engine (Pratt & Whitney Canada PW124B). The crew referred to the QRH and decided to divert to CYRT. While enroute to CYRT, the master caution light for the engine low oil pressure illuminated. The crew shut down the left engine as a precautionary measure and continued to CYRT where they carried out an uneventful landing.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionTSB
2021Thursday 24 June 202111:15 LTPiper PA-28-161 Warrior IITrident Aircraft IncN2143G28-79161761978Lycoming O-320-D3GFatalities: 0 / Occupants: 10DestroyedAccidentnear Easton/Newnam Field Airport (ESN/KESN), Easton, MD - United States of AmericaApproachTrainingEaston/Newnam Field Airport (ESN/KESN), Easton, MDEaston/Newnam Field Airport (ESN/KESN), Easton, MDThe student pilot was conducting his first solo flight. After his second takeoff, while turning onto the downwind leg of the airport traffic pattern, he heard the engine lose power. At an altitude of 700 ft above ground level, he did not think he could make it back to the airport, so he maneuvered the airplane for a forced landing to a field. During the approach, the airplane stalled and impacted a construction area before reaching the field. A postcrash fire ensued. Flight control cable continuity for the aileron, stabilator, and rudder cables were continuous from the cockpit to the respective control surfaces, except for separations consistent with recovery cuts near the wing roots and the tailcone. The engine cylinders were examined with a borescope and minor scoring was noted. No anomalies were noted with the airframe or engine that would have precluded normal operation; however, due to the extent of the postcrash fire damage, the ignition and fuel systems could not be examined or tested, and the reason for the loss of engine power could not be determined. Probable Cause: A total loss of engine power for reasons that could not be determined.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description8649 hoursERA21LA267NTSBFinal report01d79b500e2f2db5408f291583367dffInvestigation completed
2021Thursday 15 April 202110:00 LTPiper PA-22-160 PacerPrivateN3551Z22-74621960Lycoming O-320 SERIESFatalities: 0 / Occupants: 10SubstantialAccidentCottonwood Airport (P52), Cottonwood, AZ - United States of AmericaLandingPrivateCalnevar, NV (1L4)Cottonwood, AZAccident investigation report completed and information capturedThe pilot of a tailwheel equipped airplane reported that, during the landing roll, while adjusting the flap handle, he briefly stepped on the right rudder and the airplane veered to the right. While attempting to correct with left rudder input, the airplane continued to veer to the right, exited the runway, ground looped to the right and collapsed the left main landing gear. The airplane sustained substantial damage to the left wing. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. Probable Cause: The pilot's failure to maintain directional control during landing, which resulted in a ground loop.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description3400 hoursWPR21LA160NTSBFinal reportafa529e4c143c5bf50ea9a6ae1168f91Investigation completed5 months
2021Thursday 4 February 202113:20 UTCDiamond DA62PrivatePS-EBI62.0892018Fatalities: 0 / Occupants: 20SubstantialAccidentFazenda Chapadão, Barreiras, BA - BrazilLandingPrivateFazenda Vitória (SITH) Aerodrome, Luís Eduardo Magalhães, BAFazenda Chapadão, Barreiras, BAAccident investigation report completed and information capturedThe aircraft took off from the Fazenda Vitória (SITH) Aerodrome, Luís Eduardo Magalhães, BA, bound for the Agricultural Landing Area of Fazenda Chapadão, Barreiras, BA, at approximately 13:05 (UTC), with one pilot and one passenger on board. During the rollout after landing, while trying to divert from a mud puddle, the left wing collided with a corn field, resulting in loss of aircraft control. After a yaw of approximately 90 degrees to the left, the aircraft came to a stop with its front end in the cornfield.The aircraft had substantial damage. All on board were unharmed. Contributing factors. - Control skills – undetermined. It is possible that, during the reported deviation attempt, an inadequacy in the use of the controls resulted in the contact of the left-wing tip with the existing vegetation on the side of the runway, which caused an abrupt left turn, whose correction could not be performed because of the conditions prevailing at the time of landing (soft, wet, slippery terrain with accumulations of water). - Piloting judgment – a contributor. The fact that it had rained the day before and the slippery condition of the runway, in which there were still puddles of water, as well as the non-compliance with the requirements established in the RBACs 91 and 137, led the investigators to conclude that the inadequate assessment of the risks associated with the operation conducted under such conditions contributed to this accident. In addition, the requirements established in the RBACs 91 and 137 which prevented the operation in that location, were not considered.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionCENIPAFinal report279bfaa2d75a874f10032e694c195a9aInvestigation completed1 year and 8 months
2021Monday 8 November 202116:15 LTCub Crafters CC18-180 Top CubU.S. Department of the InteriorN413CCCC18-00652013Lycoming O-360-C4PFatalities: 0 / Occupants: 10SubstantialAccidentYukon Charlie River, AK - United States of AmericaLandingUnknownEagle Airport, AK (EAA/PAEG)Yukon Charlie River, AKAccident investigation report completed and information capturedThe pilot reported that he had completed one high to mid-level reconnaissance flight over the snow-covered runway in his tundra tire tailwheel-equipped airplane. Before landing, he intended to fly a low pass and drag the main landing gear along the surface of the runway to determine the depth of the snow. As the main landing gear wheels touched down atop the snow, he stated it initially felt okay but also felt deeper than what he had anticipated. He applied full power and began to apply back stick pressure, but he felt the snow consistency change to a punchy feeling, and the airplane's tail began to rise. Subsequently, the airplane nosed over and sustained substantial damage to the rudder and right-wing lift strut. The pilot reported that there were no preimpact mechanical failures or malfunctions with the airplane that would have precluded normal operation. Probable Cause: The pilot's selection of an unsuitable landing site, which resulted in a nose-over.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description1388 hoursANC22LA006NTSBFinal report2b2c26ccaa4c02318a4719ab5e388cd1Investigation completed
2021Monday 14 June 2021dayGulfstream American AA-5B TigerPrivateG-BIPVAA5B-0981Fatalities: 0 / Occupants: 10SubstantialSandown Airport, Sandown, Isle of Wight - United KingdomLandingPrivateSandown Airport (EGHN)Information verified through data from accident investigation authoritiesGulfstream American AA-5B Tiger G-BIPV substantially damaged 14 June 2021 in a landing accident at Sandown Airport, Sandown, Isle of Wight. The incident was the subject of an AAIB Correspondence-only investigation, published on 14 October 2021 and the following is the summary from that... "14 Jun 2021 Gulfstream AA-5B G-BIPV Sandown Airport, Isle of Wight, Hampshire Following an uneventful approach to land in very little wind, with full flap deployed, the aircraft floated over the grass strip for an “unusually long” time before touching down. The brakes were applied but the pilot was unable to bring the aircraft to a safe stop. It overran the end of the runway into rough terrain and gravel, during which the nose gear collapsed".You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Wednesday 14 July 2021Cessna U206G Stationair 6 IIAero JomachaXA-KCHFatalities: 0 / Occupants: 10SubstantialMorelos, Chihuahua - MexicoEn routeFerry/positioningInformation is only available from news, social media or unofficial sourcesA Cessna U206G Stationair 6 II crashed under unknown circumstances in Morelos, Chihuahua. The pilot was not injured.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Wednesday 30 June 2021c. 18:45 UTCPiper PA-23-250 Aztec FPacific Fleet Aviation LLCN1715Y27-76540961976Fatalities: 0 / Occupants: 10SubstantialAccidentKona-Keahole Airport, HI (KOA/PHKO) - United States of AmericaTaxiPrivateKona-Keahole Airport, HI (KOA/PHKO)Information is only available from news, social media or unofficial sourcesA Piper PA-23-250 Aztec F sustained substantial damage when it collided with Dassault Falcon 900C N917JF at Kona-Keahole Airport (KOA/PHKO), Hawai, USA. There were no injuries.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionNTSB
2021Monday 29 March 202116:03 UTCProgressive Aerodyne SeaRey LSAProgressive Aerodyne IncN847SR1096Fatalities: 0 / Occupants: 10UnknownFlagler County Airport, FL (FIN/KFIN) - United States of AmericaLandingPrivateFlagler County Airport, FL (FIN/KFIN)Information is only available from news, social media or unofficial sourcesAircraft landed and veered off runway into the grass, became airborne again, returned to land and veered off the runway into the grass.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Monday 15 November 2021Van's RV-3PrivateI-1174Fatalities: 1 / Occupants: 10DestroyedAccidentnear Ano Amygdali, Larissa - GreeceEn routePrivateDramaAthensLittle or no information is availableThe aircraft crashed into a heavily wooded steep ravine, killing the pilot.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Friday 10 December 202113:10Air Tractor AT-802Fatalities: 0 / Occupants:0SubstantialAccident49.8 km 286 degrees from Wee Waa, NSW - AustraliaUnknownAgriculturalInformation verified through data from accident investigation authoritiesDuring agricultural spraying operations, the aircraft struck a powerline and the pilot diverted the aircraft to Moree. The aircraft sustained substantial damage.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionATSB
2021Saturday 3 April 2021c. 15:21Robinson R22 BetaSpitzer Helicopter LLCN7434737592005Fatalities: 0 / Occupants: 20UnknownMartin State Airport (MTN/KMTN), Baltimore, MD - United States of AmericaManoeuvring (airshow, firefighting, ag.ops.)PrivateBaltimore-Glenn L. Martin Airport, MD (MTN/KMTN)Baltimore-Glenn L. Martin Airport, MD (MTN/KMTN)Information is only available from news, social media or unofficial sourcesThe aircraft experienced a tail rotor strike during hover at Martin State Airport (MTN/KMTN), Baltimore, Maryland. The helicopter sustained unreported damage and the two pilots onboard were not injured during the incident.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Sunday 9 May 202109:04Airbus A320-214Trade Air9A-BTH14542001CFMI CFM56-5B4/PFatalities: 0 / Occupants:0UnknownLjubljana Airport (LJU/LJLJ) - SloveniaTake offPassengerLjubljana-Brnik Airport (LJU/LJLJ)Madeira-Cristiano Ronaldo International Airport (FNC/LPFU)Information is only available from news, social media or unofficial sourcesTrade Air flight C3125, a Airbus A320-214, returned to land at Ljubljana Airport after suffering a bird strike. The Ljubljana Tower controller reported that airport operations located a harrier on the runway.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Wednesday 13 January 2021Mil Mi-24?Sudan Armed ForcesFatalities: 0 / Occupants: 30DestroyedWad Zayed Airport, al-Showak, al-Qadarif province - SudanTake offMilitaryWad Zayed Airport, al-Showak, al-Qadarif provinceInformation is only available from news, social media or unofficial sourcesThe Sudanese military helicopter crashed upon takeoff under unknown circumstances. All three crew members survived the crash. *media reported an Apache helicopter. Impossible as the SAF has not this helicopter and it can't carry 3 POB!This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Wednesday 13 October 202107:55Boeing 737-8AS (WL)RyanairEI-EKR38503/32022010CFMI CFM56-7BFatalities: 0 / Occupants:0Minornear Manchester Airport, Ringway, Manchester - United KingdomTake offPassenger - ScheduledManchester International Airport (MAN/EGCC)Lanzarote Airport (ACE/GCRR)Information is only available from news, social media or unofficial sourcesRyanair flight FR2131, a Boeing 737-8AS, suffered a bird strike on departure from Manchester Airport, U.K. The flight crew stopped the climb at 3625 feet and entered a holding pattern over Warrington, north of Liverpool before safely diverting to Liverpool Airport, where it landed safely on runway 27 about 55 minutes after departure. Ground observers at Manchester reported the engines (CFM56) sounded rough, almost like a helicopter, as the aircraft climbed out. A spokesperson for Ryanair said: "“This flight from Manchester to Lanzarote (13th Oct) diverted to Liverpool airport following a minor bird strike. The aircraft landed normally, and customers were transferred to a replacement aircraft which departed to Lanzarote following a short delay of approximately one hour. "Ryanair sincerely apologised to all affected customers." A Liverpool John Lennon Airport confirmed the Ryanair flight's unscheduled landing: "A Ryanair flight that took off from Manchester Airport bound for Arrecife (Lanzarote) requested to land here at Liverpool John Lennon Airport at 08:45 this morning landing safely and without incident at 08:53."This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Wednesday 12 May 202115:30Aérospatiale AS 350B2 EcureuilUS Customs and Border Protection (CBP)N841BP20361987Turbomeca Arriel 1D1Fatalities: 0 / Occupants: 20DestroyedAccidentClarence E Page Municipal Airport (RCE/KRCE), Oklahoma City, OK - United States of AmericaManoeuvring (airshow, firefighting, ag.ops.)TrainingOklahoma City-Will Rogers Airport, OK (OKC/KOKC)Clarence E Page Municipal Airport, OK (RCE/KRCE)Accident investigation report completed and information capturedOn May 12, 2021, about 1530 central daylight time, an Aerospatiale (Airbus) AS350 B2 helicopter, N841BP, was destroyed when it was involved in an accident near Yukon, Oklahoma. The pilot receiving instruction and the flight instructor were not injured. The helicopter was operated as a 14 CFR Part 91 public aircraft instructional flight. The pilot receiving instruction (pilot) and the flight instructor were conducting a training flight in the helicopter. They performed several simulated emergencies, each of which required the helicopter’s hydraulic system to be turned off and then turned back on at the conclusion of the procedure. The hydraulic system was turned off and on using the hydraulic cut-off switch, an unguarded push-button switch mounted on the end of the pilot’s collective stick. After completing the emergency procedures, the pilot performed four quick stop maneuvers. The flight instructor reported that on the last quick stop, the helicopter slowed normally but then started a left yaw about 25 ft above ground level. The pilot noted the left yaw and attempted to correct it, but his pedal inputs did not stop the yaw. As the pilot tightened his grip on the collective, the hydraulic system turned off, likely due to the pilot inadvertently pressing the hydraulic cut-off switch, and the left yaw rapidly increased to a left spin. According to the flight instructor, the control loads “instantly became excessive,” and he noticed the hydraulic light on the caution warning panel was illuminated. The pilot intentionally pressed the hydraulic cut-off switch a total of three times, but hydraulic pressure was never restored. The flight instructor told the pilot that he was taking control of the helicopter. However, the pilot did not relinquish control. The flight instructor attempted to regain control of the helicopter but was unable to overcome the high control loads. The helicopter continued to spin, impacted the ground, rolled over, and came to rest on its right side. A postimpact fire consumed most of the helicopter. Although examination of the helicopter was limited due to fire damage, no preimpact abnormalities were identified with helicopter’s airframe and engine. The US Customs and Border Protection Air and Marine Operations Division reported that the agency’s selection process for the Air Interdiction Agent Program failed to properly identify that the pilot was not qualified for the program. Because the pilot did not have the qualifications and experience required for the Air Interdiction Agent Program, he did not have the prerequisite skill necessary to critically assess the situation given by the flight instructor. This resulted in the pilot applying improper corrective actions and failing to relinquish control of the helicopter to the flight instructor when directed, which contributed the accident. Probable Cause: The pilot receiving instruction’s untimely and unidentified inadvertent activation of the hydraulic cut-off switch, which turned off the hydraulic system while the helicopter was at slow airspeed followed by a rapid power increase, which resulted in a loss of control. Contributing was the pilot’s failure to relinquish control of the helicopter to the flight instructor when directed.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description15261 hoursCEN21LA216NTSBFinal report7baa4e156c49947f85e901d3a2db324cInvestigation completed
2021Saturday 10 April 202114:30 LTCessna 150MPrivateN439WT150779171976Continental O-200Fatalities: 0 / Occupants: 20SubstantialAccidentTishomingo, Oklahoma - United States of AmericaTake offPrivateTishomingo, OKTishomingo, OKAccident investigation report completed and information capturedThe pilot reported he was taking off on personal flight when a gust of wind lifted the airplane's wing, and the airplane became airborne during his corrective control input. The pilot continued the climbout and attempted to gain airspeed, but the airplane did not accelerate and seemed to slow. The pilot elected to land the airplane to avoid trees that were ahead of him. The airplane touched down on a grass area just beyond the end of the runway but impacted in a drainage ditch about 100 ft. beyond the departure end of the runway that collapsed the nose landing gear. The airplane sustained substantial damage to the engine mounts at the nose landing gear. A Federal Aviation Administration inspector reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operations and that the engine was making power at impact. At the time of the accident, the pilot was taking off on runway 35 with a quartering wind from the northwest. The pilot reported that he may have encountered wind shear over the treetops which might have kept him low and slow to accelerate. Probable Cause: The pilot's decision to abort the takeoff on encountering a wind gust and his landing beyond the end of the runway that resulted in the airplane impacting a ditch collapsing the nose landing gear.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description5976 hoursCEN21LA188NTSBFinal report9ba0231e686c740160cb24824582fd89Investigation completed6 months
2021Tuesday 6 April 202111:30Beechcraft A36 Bonanza394 LLCN18394E-11211977Continental IO520BAFatalities: 0 / Occupants: 10SubstantialAccidentnear Arcadia Municipal Airport (X06), Arcadia, FL - United States of AmericaEn routePrivateArcadia Municipal Airport, FL (X06)Venice Municipal Airport, FL (VNC/KVNC)Accident investigation report completed and information capturedOn April 6, 2021, about 1130 eastern daylight time, a Beech A36, N18394, was substantially damaged when it was involved in an accident near Arcadia, Florida. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. Shortly after takeoff, the pilot noticed the engine rpm had increased and oil pressure was zero. While returning to the airport the engine lost all power and the pilot performed a forced landing to a field. About 8 months prior to the accident, all six cylinders were replaced. Examination of the engine revealed the engine was seized and would not rotate. The reason for the loss of power was not determined. The engine was not made available for an NTSB postaccident examination. Probable Cause: A total loss of engine power for underdetermined reasons.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description5443 hoursERA21LA174NTSBFinal reportdad9c97408df80d7ae86fa6fdacd236dInvestigation completed2 years 1 month
2021Sunday 30 May 202108:37Cessna A188AAgrícola de Servicios Aéreos del Meta - ASAMHK-147718800696Fatalities: 1 / Occupants: 10DestroyedAccidentnear El Dólar airfield, Paz de Ariporo - ColombiaManoeuvring (airshow, firefighting, ag.ops.)AgriculturalAccident investigation report completed and information capturedDuring the execution of aerial spraying activities to rice fields in the La Reforma field, located in the Municipality of Paz de Ariporo - Casanare, the Cessna A188A aircraft, registration HK-1477, lost altitude during the execution of a turn, colliding with the ground. As a result of the impact, the aircraft suffered substantial damage and its sole occupant sustained fatal injuries. The investigation determined that the accident was caused by the loss of control in flight due to the execution of a turn maneuver, which probably exceeded the aerodynamic limits of the aircraft, generating a loss of lift at low altitude and the subsequent collision with the terrain. To this cause, a contributing factor related to the existence in the area of low level wind shear (LLWS) and clear air turbulence (CAT) in the atmospheric surface layer during low altitude flights was assigned. Probable Cause(s). - Loss of control in flight originating from the execution of a turn maneuver, which probably exceeded the aerodynamic limits of the aircraft, generating a loss of lift at low altitude and the followed collision with the terrain. Contributing factors: - Existence in the area of low-level wind shear (LLWS) and clear air turbulence (CAT) in the atmospheric surface layer during low-altitude flight execution.You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident descriptionCOL-21-20-DIACCAerocivilFinal reportc708373bdd02cd6f0df247287d10620bInvestigation completed10 months
2021Tuesday 27 April 202123:00Learjet 60EmergenciasLV-HXK60-316Fatalities: 0 / Occupants:0MinorSan Fernando Airport, BA (FDO/SADF) - ArgentinaPushback / towingExecutiveSan Fernando Airport, BA (FDO/SADF)Information is only available from news, social media or unofficial sourcesThe plane was being towed along taxiway "C" to a remote location at the San Fernando International Airport (FDO/SADF), when it was hit by a van belonging to the airport operator. No injuries were reported. Material damage to the wing tip and windshield of the truck.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description
2021Saturday 29 May 2021ultralightFatalities: 0 / Occupants: 10MinorDahlemer Binz Airfield (EDKV) - GermanyLandingTrainingDahlemer Binz Airfield (EDKV)Information is only available from news, social media or unofficial sourcesThe ultralight was caught by a gust of wind. A wing hit the ground and the aircraft swerved into a meadow.This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. You can contribute by submitting additional or updated information. Corrections or additions? ... Edit this accident description

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